|
|
Photos from our 2010 SVRA at the 12-Hours of Sebring event have been posted. Also a few photos of our Mitty 2010 event have been posted.
Here are a few great photos of our race car found on www.motorsport.com :
Below are a few pictures sent to us by Richard Prince. We hope you enjoy these pictures as much as we did!
Drop us a line on our blog. If you have photos that you would like to share with us, please let us know.
May 7, 2010
There was no time for a last report prior to our departure for the Mitty, as the car was completed, well, almost completed, the night before!
Five Days Before Departure
At 10:30 at night, after installing the temporary FS5W63A gearbox, it was noted that the new clutch would not release. At this point, we feared we would not make it, but failure was not an option.
Four Days Before Departure
We made a couple of phone calls to inquire about our clutch dilemma and received similar responses regarding some flyweights used by this brand of clutch. Out comes the gearbox and clutch, again. We analyzed the problem and it was confirmed that the flyweights were interfering. The offending “extra part” was removed and all put back together – the clutch worked! We called it a day by 11:00 pm, but we still needed an exhaust pipe, a distributor, corner balancing and alignment.
Three Days Before Departure
Alex and Christian cleaned the car and trailer and took it to the muffler shop, while I worked on the new Pertronix-equipped distributor. This distributor would check OK on the bench, but the engine refused to start with it. While the car was on the rack at the muffler shop, it was noticed that one of the rear wheel stub shafts had backed out. It was very fortunate that this was noticed, as it would have been disastrous if the half shaft would have come out while on the track. The nut that holds the stub shaft had not been staked by a previous owner and had fallen out, but held captive by the U-joint flange. Luckily, there was no damage. The nut was reinstalled, torqued and staked. The other stub axle was checked and the nut was found to be tight, but not stacked. This was corrected.
Two Days Before Departure (Sunday)
After not finding any fault with the Pertronix, it was decided to build, from scratch, a dual point distributor. It was tested in our street 510 at Nestor’s house, but no time to install it in the racecar, which was at another location.
One Day Before Departure
Still running on the distributor borrowed from the old 510 wagon that saved the day at Sebring, we went to the alignment shop. Incredibly, corner balancing and suspension adjustments were uneventful! The distributor was the last planned item. It would have to be installed at the track.
Finally The Mitty
Since there was a Datsun reunion, we had to take our red 510 that we’ve owned since new. It hadn’t been on a long trip in decades, and there was only time to check tire pressures and oil level. However, we did not anticipate any problems for the 1500-mile round trip, since this car’s maintenance is always up-to-date. It ran as expected.
We enjoyed meeting so many Datsun people at the BRE dinner and Datsun corral. Factory racecars and Ron Carter’s #46 240Z replica were incredible. Meeting the original BRE Team members, legends we had only seen and heard of in magazines in the last 40 years, was also an experience not to be forgotten.
Now to the racing:
The dual point distributor ran flawlessly. Our racecar went on the track 10 times. The first time out, we noticed we had unstable fuel pressure; a new regulator corrected this. Earlier problems with the starter casting cracking came back. One cracked, then the spare cracked after only one outing. The problem appears to be caused by some vibration resonance and not just weak castings, as our newly designed alternator tensioner bracket also cracked. A replacement starter was located at an auto parts’ store 43 miles from the track. We rushed out to get it in the red 510 and got back with 20 minutes to spare. This time we tried something new to keep the starter from falling apart. It must have helped, as there were no more starter failures in the last four track outings. Weld modifications to a spare bracket for the alternator were made with the help of the Porsche folks at the 901 Shop, who were very accommodating. The modified bracket was installed at the same time as the last starter, and it also held. The car only required topping off the fuel cell for the final four track sessions.
We gradually improved our confidence as we acclimated to the new track. Changes we had made to the braking system and suspension worked, and we soon got into a good rhythm and consistent lap times. We earned second place in class on our last race on Sunday afternoon. More improvements are on the way, but finally feel we can be competitive!
We were presented with an award by none other than Pete and Gayle Brock for 2nd Place BRE Datsun 510 Tribute Car. First place went to Bob Leitzinger. This was truly an honor. Also, while looking through racecar photos at a kiosk, we found a photo of our own 510 on the track. Needless to say, we purchased it.
As always, we thank all those fans and fellow competitors who stopped by and certainly appreciate all the nice comments. Visiting with old friends we hadn’t seen in many years completed a fabulous weekend.
Until next time …
-
-
Our race car with our original 510
-
-
The team with John Morton
-
-
Brothers having fun
-
-
-
April 20, 2010
We put in a 12-hour day on Saturday and ran into some serious unexpected problems!
The failure of the Spec clutch was the release of one of the three flat springs that locate the pressure plate. It caused extensive shrapnel damage and was replaced, together with a restored Tilton flywheel as a balanced assembly, during the week.
We designed, manufactured and installed a very nice adapter for the rear gearbox mount. We had been told, by the supplier who repaired the damaged 5th gear synchro and associated parts in the direct drive gearbox, that everything looked good and that every gear would engage. We didn’t check this ourselves before installing it, but once we did, we found it would not go into the reverse gate. The gearbox came out again last night. In its place, a gearbox from one of our street 510s was installed; there’s no time for repairs. This third box is a Model FS5W63A, as used in the 1979 Datsun 200SX and HL510. It has wider ratios than we would like, but at least it was restored by ourselves two years ago and should be reliable. After a full day at the office, last night we worked on the gearboxes removals (2 ea.) and installation (1 ea.) for another eight hours. We, again, have to work on the rear mount adapter; the donor car was a wagon and there are apparent differences. The shifter hole on the floor also needs to be moved further forward than with any of the two previous gearboxes.
Also, a newly refurbished ignition distributor with a new Pertronix igniter will not produce any spark.
Once we solve the gearbox and ignition problems, we still have to reshape the exhaust pipe to clear the rear mount, make suspension alignment changes, finish other minor stuff, do a test drive on our front street and load the trailer for the 12-hor drive to the Mitty. Hope we can get some sleep before our scheduled departure.
As race spectators, we used to think that those who start working on their cars the moment they get to the track were those who were unprepared. Now, as competitors, we fully understand why.
We’ll report again before departing for the Mitty at Road Atlanta.
April 7, 2010
We had mentioned that we were planning on making suspension adjustments to our Datsun 510 racecar, but we didn’t touch on the subject in our last post. Well, we think we’re heading in the right direction. The car is more stable during hard braking. The next adjustment before the Mitty at Road Atlanta at the end of the month will be to improve cornering. But first, we must do a clutch and gearbox change.
The failing roadster gearbox has been removed and some issues with the clutch were identified. A new clutch will be balanced with the Tilton flywheel as an assembly before installation.
While waiting on parts for the gearbox change, we’ll be replacing the gauges. As I mentioned much earlier, first we had difficulty calibrating the Stewart-Warner tachometer. Rather than continue wasting time with the tach, replacing it with an Autometer tach fixed that problem. During our last Sebring run, another gauge failed, so we’re going to liquid filled Autometer throughout.
The fuel pump inertia cut-off switch had also given problems, tripping for no apparent reason. A new unit did not perform any better, and our driver related feeling like an octopus, between resetting the switch and dealing with a very hard to shift gearbox. The inertia switch may sound like a good safety feature, but it’s out of the car. If someone knows of a reliable switch, please let us know.
The failure of the distributor shaft bushing has been confirmed. It was caused by neglect from a previous owner, who assembled it completely dry. With proper maintenance, I have put well over 330,000 road miles in one and over 220,000 miles in another of these distributors without any wear problems. A replacement is now ready for installation.
The Option 1 direct drive gearbox Model F5C71B has been repaired and will be installed this week. There was not enough time at this moment to do a full inspection/overhaul. The apparent root cause of it’s failure at Sebring, while on loan to Bob Leitzinger, was that the supplier who sold it to Moya Motorsports assembled it with a damaged input shaft, which caused the 5th gear synchro to come appart.
Lots of work planned for this week. We’ll report on the progress made through this weekend by early next week.
Where do I start! Pete Brock of BRE fame, who ran the Factory Datsun Trans-Am Team in the early ‘70s, stopped by with his wife, Gayle. They were very supportive of our effort, spent a long time with us and gave us some pointers. We had some unexpected problems on track with systems that had not been touched since we got the car. These problems are a testament of how much development a new racecar requires.
Problem #1: Gear selection has been a problem and has gotten worse. We suspect it may be costing several seconds per lap. We expect to have the direct drive Option 1 F5C71B gearbox for the Mitty at Road Atlanta at the end of April. The new gearbox has some history; more on this later.
Problem #2: An apparent failure of the distributor shaft bushing allowed the shaft to wobble, causing damage to the Pertronix unit; we came in the pits in the 1/2-hour race and DNF with a lap to go. This was very unfortunate, as we were having a good run with Orie Voightmann in another Datsun 510. We had meant to rework the failed distributor prior to to this event, but ran out of time. A spare distributor, a points unit borrowed from my street 510 wagon that was back in Miami, got us going for the parade laps when the only issue was the difficulty in shifting gears.
Back to the gearbox. The direct drive gearbox is another component we have wanted to install at first opportunity. That opportunity has come, since we’re not going back on track with the worn roadster box. Anyway, the new gearbox had not been tested and, when none other than Bob Leitzinger had his own gearbox fail during practice, we offered ours, and a propeller shaft that goes with it, so he could finish the weekend. We were very happy to be able to help him get back on the track and, since we knew he would not abuse the unit, also felt it was an excellent opportunity to test our new box. Bob went on track the next day for the 1-hour enduro and took our class win with our gearbox! Then, during the Friday 1/2-hour race as we came into the pits a lap from the finish due to our distributor problem, Bob also came in just in front of us … The borrowed gearbox would not go into 5th, and he decided not to risk further damage. Bob wanted to pay for the repairs, but we declined his generosity knowing it wasn’t his fault. We’re glad that this had happened before we fitted it to our car.
The direct drive gearbox was purchased from a supplier in California; after waiting almost 10 months for it to be overhauled, it lasted for only two track outings. We are repairing it ourselves this time.
I have been attending Sebring as a spectator since 1982, and the rest of the team (my two sons) since they were 8 or 9 years old. We have always had a great time, but this time as competitors was the best of all — in spite of all the work during the evenings to get the car back on track.
Thanks to all the dozens of people that visited and chatted with us.
Oh, and how could I forget. We signed our first autograph! See you at the Mitty.
-
-
-
Friends supporting our effort!
-
-
-
-
-
-
-
-
-
-
-
-
-
-
-
-
-
-
Team owner and driver with Pete Brock
A big thanks to Kim & Bobby, also to Jame for the photos.
There’s been a two-month layoff since our first race, but we certainly haven’t been idle.
We were hoping to have our direct-drive gearbox and the higher gearing differential installed for the SVRA vintage race during the 12 Hours of Sebring weekend, but decided not to rush this job and will postpone it until after the Mitty at Road Atlanta at the end of April.
The opportunity to get meaningful tire temperature data has not been available, but we went ahead and made some changes to the front and rear suspension in search of better handling.
All our in-between-race scheduled checks and maintenance have been completed. The leakdown results were the same as before our first race–a good sign.
During routine inspection under the distributor cap, it was noticed that the witness marks of the arching from the rotor tip to the four cap posts were at the very tip of the posts. Also, there was evidence of arching from the cap center contact to the rotor. This indicated the rotor height was too short. The suspicion was confirmed after checking a few dimensions. It was discovered that the rotor that came with the car when it was purchased, although it appeared to be new, was actually for a standard PL510 distributor, not for the L20b distributor. A new, correct P/N rotor put this right.
The gaps on all four Champion C57 sparkplugs had widened somewhat and, while resetting the gaps, a crack was discovered on the inside radius of the ground electrode of one of the plugs. We were lucky it didn’t break off in the engine. The color of the C57s was good, but our new spare set was Champion C59 (one step warmer). The C59 plugs have been installed, and we will do a plug check after our practice run at Sebring.
The issue of the Champion plug ground electrode crack is very disturbing, as we had never experienced structural failure of a plug before. We have purchased a set of NGK R5671A-10 and NGK R5371A-9, which are of similar heat range as the Champions. The NGKs have been gapped and index-marked and are ready for action.
It was noticed, during the gapping process, that the force required to change the gap on the NGK plugs is much higher than on the Champion plugs. This indicates, at least in this respect, that the NGK sparkplugs are more robust than the Champion sparkplugs.
We plan to do our practice at Sebring with the Champion C59 currently installed to get a comparative plug reading. From then on, the “Champion” logos may remain on our BRE Tribute car, but we’ll run NGK exclusively.
We have ordered a second set of Panasport wheels to replace the American Libres currently on the rain tires. This will make tire changing easier, as the the lugs for the Panasport and Libres are not interchangeable. The Libres are genuine aluminum race wheels in excellent condition. They have glossy black spokes and clear rims, and we plan to sell them.
A change in our yellow Datsun 510 car number from 33 to 38 was required for this next race. If you’re at Sebring next week, stop by our trailer and say hello.
We completed the 2009 December Sebring HSR event; we had a blast! There was lots of rain, but, by Sunday, it had cleared and the temperature had dropped from the 70s to the 40s. We actually ran only one practice session in moist conditions. For our first race on Saturday, it looked like the rain would not stop, so we changed to our rain tires, then went back to the dry set one hour before the race.
Our first priority was to finalize our Weber 45 DCOE jetting before the first of two races. We had done some preliminary tests and had made changes to the idle jet, emulsion tube and pump jet, and expected to only make changes to the mains and air correctors at the track. The process went as planned, although it took a bit longer than we had planned. We made stepped changes (three total), then removed the NGK A/F instrumentation.
A couple of minor problems during our first testing session were corrected, then the car went on track five times, requiring only topping off the fuel cell. The two mentioned problems were, in a way, almost comical. Firstly, our new shift knob with the Datsun logo came off in the driver’s hand. Then almost immediately, the driver lost the throttle … literally. The pedal plastic hinge broke and the pedal fell off! The driver completed the session, but heeling and toeing was out of the question.
We replaced the shifter knob and made a quick trip to the hardware store for a brass hinge to repair the gas pedal. Although we had a new gas pedal back home, we think the repaired part has some character to it; maybe we’ll leave it on.
Another problem that was noticed after our second test session was with a new reduction gear starter we had installed a few weeks earlier. The aluminum casting must have been defective and a crack developed that progressed almost all the way around. Luckily, Christian noticed the crack while doing routine checks. We had a spare starter and were lucky that the cracked starter didn’t unzip completely and dropped off on track.
We were hoping to complete our tire temperature checks to arrive at final front and rear settings for camber and toe. Unfortunately, setting the carburetors took longer than anticipated and the only time we had to take tire temperature readings was during a test session, when it was cool and moist, and the tires didn’t really get up to temperature. This will be one of our main priorities for our next race.
Our goal in Vintage Racing is to always keep improving, and this we did. This was our third visit (the two earlier visits were just track tests) to Sebring with this car. Our fastest lap time has improved with each visit. We plan to make more suspension adjustments to improve our handling.
During our first race, we were excited that the very first pass we made in actual competition was on a very nice vintage Aston Martin. We passed a few other cars, but during the last lap, we put two wheels off coming out of turn 1. Instead of easing the car back on track, we forced it and this caused us to spin. We think we followed the proper procedure of ”when you spin, both feet in”, but we must not have been quick enough, as the engine stalled. Although the engine restarted right away, we had to wait for traffic and I think this put us dead last. However, we caught up and were able to make a pass on the car ahead on Turn 17 before the checkered.
The Sunday race started in very cold weather, and we were careful not to make mistakes with the cold tires. With each lap we picked up the pace, but at about the halfway point a problem, that later turned out to be very simple, stumped us at the moment and resulted in a DNF. The engine sputtered a couple of times, then quit. We later found that the inertia safety switch tripped and shut off our fuel pump. We were more ticked off at not realizing this at the moment and not being able to correct the problem on-track than we were about the actual malfunction, as the switch is resettable from the driver’s seat.
We went to the track prepared and it paid off, as we were able to deal and correct our problems.
We want to thank all those who stopped by and all the compliments we received. We’ll be back at Sebring for our next event, which will be with SVRA, during the 12-hour weekend in March 2010.
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
-
-
HSR Sebring 2009 – Moya Motorsports
The Webers have been refurbished and installed. The fuel pressure regulator was adjusted to Weber specs and the engine fired right up. We’ll do some preliminary jetting, with the aid of the A/F meter, on our street this weekend (hope the authorities don’t show up, or at least are understanding if they do appear). Final jetting selection will have to be completed at the track.
Our #33 is now a BRE Tribute Car (Re: http://bre2.net/index.php?section=116 ).
· Found why throttle would not return to idle. The front carburetor accel. pump rod came out of throttle shaft lever and jammed on carb. body. Earlier troubleshooting did not discover the problem because apparently, the rod fell back in place when throttle was moved.
· Due to the throttle jamming problem, we could not get more than two hot laps before our temporary repair would let the throttle jam again. In retrospect, we should have cut off the offending pump rod for completing the remainder of our test.
· Mikuni pump rod parts are NLA. Although we can remove the carburetors and make permanent repairs, we’ve decided we are going to replace the Mikunis with Weber 45 DCOEs.
· Lap times: Due to our throttle problem, we could only get two hot laps during the last two sessions (the first two sessions were for bedding brakes, adjusting brake bias, setting suspension, etc). We recorded a significant improvement in lap times over our June test.
· Replacement of the Stewart-Warner PN 114018 tachometer with an Autometer PN 6801 was successful. Stewart-Warner Tech Help could not come up with a solution to make their tach. work with the MSD ignition box.
· Change to softer rear springs had good results. The rear anti-roll bar was left at its softest setting, but we increased the damping on the rear shocks.
-
-
NASA Sebring 2009 – Moya Motorsports
-
-
NASA Sebring 2009 – Moya Motorsports
CLICK HERE to see some photos of the event.
|
|